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- 200W+50W Bi-Amp Power Section and Crossover Replacement For Advent Powered Speakers.
- Darker Downtime…
- Curiously Strong Power Supply Design
- ATTiny44 Based Shifty VU Meter Controller (MAKE2008)
- Curiously Strong TriAmp Speaker Selection
- Grow LED Array Rev.2 Results AKA Why Rev.3
- Grow LED Array Prototype Rev. 2
- MAKE 2008 Grow LEDs Array Prototype Design
- Stereo Audio IO Landing Pad for Olimex SAM7-H256: Assembled
- Jabra BT125 Bluetooth Headset Teardown
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200W+50W Bi-Amp Power Section and Crossover Replacement For Advent Powered Speakers.
So this thing is assembled and working, tested at about 95% non-fail. The owner is happy, and I would like to thank him again for giving me the opportunity to design his replacement amp. I think it looks pretty sexy all assembled and glowing.
The replacement boards are for a late 70s bi-amplified powered speaker made by Advent. They were funded by the speaker’s owner, Christopher Jensen, who wanted a set of amplifiers with more stability in high temperature conditions; The finished boards represent a couple months of collaborative effort. Our solution was using five National Semiconductor LM3886 Overture chip-amps (a higher output version of the LM3875 “Gainclone” chips): one chip (50W RMS) for the tweeter driver and four in bridged-parallel configuration (200W RMS) to drive the woofer. Later it was decided to build the crossover into the system instead of using the original system’s crossover board.
The design for the high channel is a straight forward LM3886 non-inverting amplifier with an AC coupled input circuit. For the bridged parallel amplifier we used the Fig. 11 BPA-200 design from National’s BPA-200 Application Note, which includes the servo amplifiers for output voltage offset compensation and uses the LM3886 in both inverting and non-inverting modes.
The boards were done in 2oz. copper and black soldermask, with integrated fuses and reverse voltage protection diodes. All high power speaker connections were done with .250″ Fast-On connector tabs. Signal inputs use RCA jacks. Rails for the LM3886 are about 1/2″ wide, running along the edges of the PCB, with a pair of 1000uF Panasonic FM series caps on each rail at each chip-amp. 2200uF FC series caps will fit into the same location. Power for the servos and buffer amp was provided by fixed +15V and -15V linear voltage regulators. The unregulated supply was also replaced, using a 500VA Avel toroid transformer, and very large electrolytic capacitors (they’re like soda cans).
The crossover circuit is integrated into the amp as a module with 0.1″ pitch headers for signal and power and locations for standoff mounting. The power section board can be used with or without the crossover, both amplifiers and the crossover have RCA input connectors. Two different crossover module boards were designed: one based off a 2-pole Linkwitz-Riley active crossover circuit, another using a 4-pole Linkwitz-Riley active crossover. Both include an input buffer before the active filters, and a simple comparator circuit with adjustable reference for driving a clip detector LED.
During design, a potentiometer for volume was added to the inputs when the crossover module was added. This makes the LPF designed into input change roll-off frequency with adjustments of volume, although in later designs this can be fixed by replacing the amp’s input resistor with the attenuator pot, unlike how it is now, before the input circuit filters and coupling. The LPF in the input circuit can also be sensitive to different source impedance. This circuit can easily be eliminated with 1206 jumper and omitting a capacitor. Also Christopher used a cap in series with the feedback divider on the high channel power amp to get its output voltage offset similar to the less than 1mV values of the servo-stabilized bridged-parallel low channel amp. He stood the 1206 resistor and capacitor up so both they fit onto the resistor pad. For this to work on the lower frequency amp or full range amps, you would need a very large value bi-polar capacitor.
I’m told pictures of the re-assembled powered speaker will be available as soon as the silicone sealer stuff dries. I guess for the rear panel, or speakers, or something. Those pics and possibly also circuit schematic and PCB layouts in later posts.
Posted by rmrubin
Posted in: Electronics
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October 2008
Darker Downtime…
So if this was a blog, I would put a whole bunch of personal stuff here about why I haven’t posted in so long. Not all of it bad, indeed some very new and exciting things have happened, too. What I will say is that Wordpress and my hosting have been sources of frustration, however for the time being it looks like this is what I am stuck with. You get what you pay for, and in terms of value im still doing better than average.
Despite the lack of posts, work on Darker Technologies has progressed between the mundane tasks of daily living. The next few posts will cover some of the work I have completed on the Curiously Strong and GrowLEDs projects, as well as related contracted work and research involving audio PCBs, and of new things to come.
Put on your seatbelts.
Posted by rmrubin
Posted in: Electronics
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September 2008
Curiously Strong Power Supply Design
18VAC dual secondary 160VA toroid into a full wave rectifier with 32*470uF caps, for about 5.5Vpp ripple at 10A. Rectified output is fed into four MC34063 based SMPS supplies, three step-down and one inverting. The outputs of the SMPS are fed into 5 linear regulators, for a 15V bipolar rails, 15V power amp rail, 10V small amp rail, and 6V shifty VU rail. Designs are compatible with non through hole plate boards. All boards will be fabricated on a Taig 2019CR CNC mill.
Posted by rmrubin
Posted in: Make2008, Electronics
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April 2008
ATTiny44 Based Shifty VU Meter Controller (MAKE2008)
Schematic and circuit board design for the Shifty VU Controller. Designed for an Altoids tin chassis, the analog section includes a stereo full-wave rectifier made with a quad rail-to-rail opamp, with logic FET switched capacitors to adjust the rectifier output’s rolloff delay.
shifty_vu_controller_schema.png
Posted by rmrubin
Posted in: Make2008, Electronics
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April 2008
Curiously Strong TriAmp Speaker Selection
Tang Band drivers from Parts Express. 300Hz and 5KHz look good for crossover. $2 Goldwood tweeters. Not worth posting (even if they did have specs, which they don’t). Chassis is planned to be laser cut acrylic (!) courtesy of macetech and Techshop. A high density cardboard concrete/plaster casting tube may be integrated into the design as a waveguide for the 5″ driver. Open Baffle mid drivers are also being considered.
Posted by rmrubin
Posted in: Make2008, Electronics
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April 2008
Grow LED Array Rev.2 Results AKA Why Rev.3
Why Rev.3?
- Topside ground plane connection underneath connector. Inaccessible, non functional without thru-hole plating without wire cludge.
- White rail dissipation in PNP pass transistors very far beyond spec. Red rail to spec only below 25C ambient.
- Transition to ethernet input.
Short term testing of hardware observations:
- Normal room temp.
- 25V unregulated psu.
- All circuits function as intended.
- Red and blue series transistors warm to touch.
- White series transistor hot set at 1/2 normal current.
Conclusions:
- Multiple rail PSU, <0.8V overhead at max string Vf. Blue rail is an example. Benefit is less dissipation per output.
- SOT223 instead of SOT23 3906 series transistors. Same dissipation but within spec. Benefit is single-rail lower-cost psu and a sexier transistor package.
- Dropping resistors for white and red LED rails. electrically same as SOT223 dissipation, retain cheaper SOT23 package.
- Higher dissipation SOT23 PNP for red rail viability without resistor. Must test at higher ambient.(MMBT4403?)
- Three channels current feedback SMPS. Much less dissipation, psu same level complication as tri rail. Cost benefit unknown.
Paper Test:
LED Vf(max)
Red =2.4
Blue =3.6
White =3.6
LED Vf(typ)
Red =1.7
Blue =2.8
White =2.8
String Vf(max)
8x Red =19.2
6x Blue =21.6
2x White =7.2
String Vf(typ)
8x Red =13.6
6x Blue =16.8
2x White =5.6
String W(max) @ 20mA
8x Red =0.384
6x Blue =0.432
2x White =0.114
String W(typ) @ 20mA
8x Red =0.272
6x Blue =0.336
2x White =0.112
System Output W(max) @ 20mA
4x Red Strings =1.536
3x Blue Strings =1.296
1x White Strings =0.228
RB Total =2.832
RBW Total =3.060
System Output W(typ) @ 20mA
4x Red Strings =1.088
3x Blue Strings =1.008
1x White Strings =0.288
RB Total =2.096
RBW Total =2.384
MMBT3904 Vce(max) @ 23V V[supply]-Vf[string_max]-Vbe[0.6V]
Red =3.2
Blue =0.8
White =15.2
MMBT3904 Vce(typ) @ 23V V[supply]-Vf[string_typ]-Vbe[0.6V]
Red =8.8
Blue =5.6
White =16.8
MMBT3904 mW(max) @ 23V/20mA
Red =64
Blue =16
White =304
MMBT3904 mW(typ) @ 23V/20mA
Red =176
Blue =112
White =336
MMBT2904 Temp(max) @ 23V/20mA 357C/W
Red =22.848
Blue =5.712
White =108.528
MMBT3904 Temp(typ) @ 23V/20mA 357C/W
Red =62.832
Blue =39.984
White =119.952
MMBT3904 mW_derate(max) 23V/20mA Ambient 25C 2.8mW/C
Red =63.9744
Blue =15.9936
White =303.8784
MMBT3904 mW_derate(typ) 23V/20mA Ambient 25C 2.8mW/C
Red =175.9296
Blue =111.9552
White =335.8656
MMBT3906 mW_overhead(max) 23V/20mA/25C 350mW[SOT23]-mW_derating-mW_used
Red =223
Blue =319
White =-257(!)
MMBT3906 mW_overhead(typ) 23V/20mA/25C 350mW SOT23
Red =-1
Blue =127
White =-321(!)
MMBT3906 Source, Vf(max)/If=20mA/23V/25C/77F
Red = OK
Blue = OK
White = FAIL
MMBT3906 Source, Vf(typ)/If=20mA/23V/25C/77F
Red = ALMOST, BUT FAILED
Blue = OK
White = FAIL
Posted by rmrubin
Posted in: Electronics
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April 2008
Grow LED Array Prototype Rev. 2
Button pinouts were mirrored. Both switch channels of the button were used in order to reduce single element through current. Single-sided routing was dropped in order to pass DRC at 20mil. No benefits of single sided besides challenge, as most fab houses do not seem to care. The higher resolution boards were difficult to toner etch properly with my level of skill. The lower resolution will allow for easier etching and milling with tools at hand. A pair of arrays will be made in each method, in order to compare milled and etched PCB technologies. Some LED pins must be soldered top side due to lack of through hole plating.
Posted by rmrubin
Posted in: Electronics
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March 2008
MAKE 2008 Grow LEDs Array Prototype Design
Single sided board design for an array of 24 blue, 24 red, and 2 white LED. For use as small plant lighting. Switching (SMPS) power supply and optional digital control unit are external, and support a minimum of 2 arrays. The white LED are switched with a latching button. Series strings of LED are brightness regulated using MMBT3906 based current sources for immunity to poorly matched Vf and variable supply voltages, 8 blue LED and 6 red LED per string. This setup will be powered by 24V rails, to provide headroom for the LED strings at Vf(max) and and 1V needed by the current regulators. A control unit will modulate power with PWM switching at greater than 200Hz, and be capable of simulating day/night cycles, movement of the sun from horizon to horizon, and adjusting the red and blue light balance.
Posted by rmrubin
Posted in: Electronics
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March 2008
Stereo Audio IO Landing Pad for Olimex SAM7-H256: Assembled
CNC milled dual channel audio input/output board for the Olimex SAM7-h256 and SAM7-H64 header boards. Input is through an AC-coupled preamp with a single-pole bandpass input with attenuation into a rail to rail opamp in voltage follower configuration. -3db response was simulated at 2Hz-30KHz. A though port is provided to use the device an an audio monitor. Output is a pair of SAM7 PWM through a 4-pole active low-pass filter. Configuration is butterworth salen-key at 10KHz. High end audio hurts. The LED VU display is unbuffered, running at about 2.4 mA, about half a mA beyond spec for 4 of those pins. Headers are provided for asynchronous RS232 comm and external 3.3V supply. Currently it gets power from the USB.
Posted by rmrubin
Posted in: Electronics
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February 2008
Jabra BT125 Bluetooth Headset Teardown
Two very small torx screws, edge snaps, some plastic hooks at the end with mating feature on the opposite chassis piece. Speaker is insulated from the main chassis by a rubber-like pad. The mic is built into a pod made of the same rubbery material, which when mounted fits flush with the outer chassis. Torx screws came out with a clipped xacto blade tip.
Going to swap the blue 0603 LED for a red one. Maybe amber. Will possibly swap the 0402 resistor with a larger one. Try to kill the sniper beacon blink effect. Alternative is a thick film or thin paper light filter behind the translucent white button.
The grid is .250″.
Posted by rmrubin
Posted in: Electronics
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February 2008